On Wed, 19 Jun 2019 16:04:43 +0800 masonccyang@xxxxxxxxxxx wrote: > Hi Boris, > > > > > Re: [PATCH v3 2/4] mtd: rawnand: Add Macronix MX25F0A NAND controller > > > > On Tue, 18 Jun 2019 08:14:36 +0200 > > Boris Brezillon <boris.brezillon@xxxxxxxxxxxxx> wrote: > > > > > > > > > > > > > > > > > > How to make all #CS keep high for NAND to enter > > > > > > > > low-power standby mode if driver don't use > "legacy.select_chip()" > > > > ? > > > > > > > > > > > > > > See commit 02b4a52604a4 ("mtd: rawnand: Make ->select_chip() > > > > optional > > > > > > > when ->exec_op() is implemented") which states: > > > > > > > > > > > > > > "When [->select_chip() is] not implemented, the core > is > > > > assuming > > > > > > > the CS line is automatically asserted/deasserted by the > driver > > > > > > > ->exec_op() implementation." > > > > > > > > > > > > > > Of course, the above is right only when the controller driver > > > > > supports > > > > > > > the ->exec_op() interface. > > > > > > > > > > > > Currently, it seems that we will get the incorrect data and > error > > > > > > operation due to CS in error toggling if CS line is controlled > in > > > > > > ->exec_op(). > > > > Oh, and please provide the modifications you added on top of this patch. > > Right now we're speculating on what you've done which is definitely not > > an efficient way to debug this sort of issues. > > The patch is to add in beginning of ->exec_op() to control CS# low and > before return from ->exec_op() to control CS# High. > i.e,. > static in mxic_nand_exec_op( ) > { > cs_to_low(); > > > > cs_to_high(); > return; > } > > But for nand_onfi_detect(), > it calls nand_read_param_page_op() and then nand_read_data_op(). > mxic_nand_exec_op() be called twice for nand_onfi_detect() and > driver will get incorrect ONFI parameter table data from > nand_read_data_op(). And I think it's valid to release the CE pin between read_param_page_op() (CMD(0xEC)+ADDR(0x0)) and read_data_op() (data cycles) if your chip is CE-dont-care compliant. So, either you have a problem with your controller driver (CS-related timings are incorrect) or your chip is not CE-dont-care compliant. ______________________________________________________ Linux MTD discussion mailing list http://lists.infradead.org/mailman/listinfo/linux-mtd/