Hi Jonas, On 9/4/2023 2:00 AM, Jonas Gorski wrote: > If a transaction times out, the START_BUSY signal may have gotten stuck, > and subsequent transactaction attempts will fail as the bus is still > considered busy. > > To work around this, check if the START_BUSY bit is still asserted, and > reset the controller in case it is. > > This is also done by the alternative, non-upstream iproc-smbus driver > implementation [1]. > > Works around situations like: > > bcm-iproc-2c 1803b000.i2c: transaction timed out > bcm-iproc-2c 1803b000.i2c: bus is busy > bcm-iproc-2c 1803b000.i2c: bus is busy > bcm-iproc-2c 1803b000.i2c: bus is busy > bcm-iproc-2c 1803b000.i2c: bus is busy > bcm-iproc-2c 1803b000.i2c: bus is busy > ... > > where the bus never recovers after a timeout. > > [1] https://github.com/opencomputeproject/onie/blob/master/patches/kernel/3.2.69/driver-iproc-smbus.patch > > Fixes: e6e5dd3566e0 ("i2c: iproc: Add Broadcom iProc I2C Driver") > Signed-off-by: Jonas Gorski <jonas.gorski@xxxxxxxx> > --- > The iproc-smbus driver does some additional checks/mitigations, but > since my I2C understanding is only very rudimentary, I didn't add them, > also the reset was enough to fix the issue I was seeing. > > I was a bit conflicted about the Fixes tag, but since it fixes/work > around misbehaviour seen I decided to add one. > > The issue was happening only in production, and only once per boot (so > far), but with 100% probability within a few hours. > > drivers/i2c/busses/i2c-bcm-iproc.c | 9 +++++++++ > 1 file changed, 9 insertions(+) > > diff --git a/drivers/i2c/busses/i2c-bcm-iproc.c b/drivers/i2c/busses/i2c-bcm-iproc.c > index 05c80680dff4..69f9c199fa3b 100644 > --- a/drivers/i2c/busses/i2c-bcm-iproc.c > +++ b/drivers/i2c/busses/i2c-bcm-iproc.c > @@ -796,6 +796,15 @@ static int bcm_iproc_i2c_xfer_wait(struct bcm_iproc_i2c_dev *iproc_i2c, > if (!time_left && !iproc_i2c->xfer_is_done) { > dev_err(iproc_i2c->device, "transaction timed out\n"); > > + /* check if START_BUSY did not clear */ Can you please rephrase the comment to make it more clear? For example, something like this: /* * If START_BUSY is still not clear, it means the controller may have * been stuck. In this case, reset the controller to recover. */ > + if (!!(iproc_i2c_rd_reg(iproc_i2c, M_CMD_OFFSET) & > + BIT(M_CMD_START_BUSY_SHIFT))) { > + /* re-initialize i2c for recovery */ > + bcm_iproc_i2c_enable_disable(iproc_i2c, false); > + bcm_iproc_i2c_init(iproc_i2c); > + bcm_iproc_i2c_enable_disable(iproc_i2c, true); > + } > + > /* flush both TX/RX FIFOs */ > val = BIT(M_FIFO_RX_FLUSH_SHIFT) | BIT(M_FIFO_TX_FLUSH_SHIFT); > iproc_i2c_wr_reg(iproc_i2c, M_FIFO_CTRL_OFFSET, val);
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