[PATCH AUTOSEL 5.18 20/53] hamradio: 6pack: fix array-index-out-of-bounds in decode_std_command()

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From: Xu Jia <xujia39@xxxxxxxxxx>

[ Upstream commit 2b04495e21cdb9b45c28c6aeb2da560184de20a3 ]

Hulk Robot reports incorrect sp->rx_count_cooked value in decode_std_command().
This should be caused by the subtracting from sp->rx_count_cooked before.
It seems that sp->rx_count_cooked value is changed to 0, which bypassed the
previous judgment.

The situation is shown below:

         (Thread 1)			|  (Thread 2)
decode_std_command()		| resync_tnc()
...					|
if (rest == 2)			|
	sp->rx_count_cooked -= 2;	|
else if (rest == 3)			| ...
					| sp->rx_count_cooked = 0;
	sp->rx_count_cooked -= 1;	|
for (i = 0; i < sp->rx_count_cooked; i++) // report error
	checksum += sp->cooked_buf[i];

sp->rx_count_cooked is a shared variable but is not protected by a lock.
The same applies to sp->rx_count. This patch adds a lock to fix the bug.

The fail log is shown below:
=======================================================================
UBSAN: array-index-out-of-bounds in drivers/net/hamradio/6pack.c:925:31
index 400 is out of range for type 'unsigned char [400]'
CPU: 3 PID: 7433 Comm: kworker/u10:1 Not tainted 5.18.0-rc5-00163-g4b97bac0756a #2
Hardware name: QEMU Standard PC (i440FX + PIIX, 1996), BIOS rel-1.14.0-0-g155821a1990b-prebuilt.qemu.org 04/01/2014
Workqueue: events_unbound flush_to_ldisc
Call Trace:
 <TASK>
 dump_stack_lvl+0xcd/0x134
 ubsan_epilogue+0xb/0x50
 __ubsan_handle_out_of_bounds.cold+0x62/0x6c
 sixpack_receive_buf+0xfda/0x1330
 tty_ldisc_receive_buf+0x13e/0x180
 tty_port_default_receive_buf+0x6d/0xa0
 flush_to_ldisc+0x213/0x3f0
 process_one_work+0x98f/0x1620
 worker_thread+0x665/0x1080
 kthread+0x2e9/0x3a0
 ret_from_fork+0x1f/0x30
 ...

Reported-by: Hulk Robot <hulkci@xxxxxxxxxx>
Signed-off-by: Xu Jia <xujia39@xxxxxxxxxx>
Signed-off-by: David S. Miller <davem@xxxxxxxxxxxxx>
Signed-off-by: Sasha Levin <sashal@xxxxxxxxxx>
---
 drivers/net/hamradio/6pack.c | 9 ++++++++-
 1 file changed, 8 insertions(+), 1 deletion(-)

diff --git a/drivers/net/hamradio/6pack.c b/drivers/net/hamradio/6pack.c
index 45c3c4a1101b..9fb567524220 100644
--- a/drivers/net/hamradio/6pack.c
+++ b/drivers/net/hamradio/6pack.c
@@ -99,6 +99,7 @@ struct sixpack {
 
 	unsigned int		rx_count;
 	unsigned int		rx_count_cooked;
+	spinlock_t		rxlock;
 
 	int			mtu;		/* Our mtu (to spot changes!) */
 	int			buffsize;       /* Max buffers sizes */
@@ -565,6 +566,7 @@ static int sixpack_open(struct tty_struct *tty)
 	sp->dev = dev;
 
 	spin_lock_init(&sp->lock);
+	spin_lock_init(&sp->rxlock);
 	refcount_set(&sp->refcnt, 1);
 	init_completion(&sp->dead);
 
@@ -913,6 +915,7 @@ static void decode_std_command(struct sixpack *sp, unsigned char cmd)
 			sp->led_state = 0x60;
 			/* fill trailing bytes with zeroes */
 			sp->tty->ops->write(sp->tty, &sp->led_state, 1);
+			spin_lock_bh(&sp->rxlock);
 			rest = sp->rx_count;
 			if (rest != 0)
 				 for (i = rest; i <= 3; i++)
@@ -930,6 +933,7 @@ static void decode_std_command(struct sixpack *sp, unsigned char cmd)
 				sp_bump(sp, 0);
 			}
 			sp->rx_count_cooked = 0;
+			spin_unlock_bh(&sp->rxlock);
 		}
 		break;
 	case SIXP_TX_URUN: printk(KERN_DEBUG "6pack: TX underrun\n");
@@ -959,8 +963,11 @@ sixpack_decode(struct sixpack *sp, const unsigned char *pre_rbuff, int count)
 			decode_prio_command(sp, inbyte);
 		else if ((inbyte & SIXP_STD_CMD_MASK) != 0)
 			decode_std_command(sp, inbyte);
-		else if ((sp->status & SIXP_RX_DCD_MASK) == SIXP_RX_DCD_MASK)
+		else if ((sp->status & SIXP_RX_DCD_MASK) == SIXP_RX_DCD_MASK) {
+			spin_lock_bh(&sp->rxlock);
 			decode_data(sp, inbyte);
+			spin_unlock_bh(&sp->rxlock);
+		}
 	}
 }
 
-- 
2.35.1




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