Hi,
On Mon, 12 Feb 2024, Nam Cao wrote:
On 12/Feb/2024 Moritz C. Weber wrote:
Fixed a code style issue raised by checkpatch.
---
drivers/staging/nvec/nvec.c | 4 ++--
1 file changed, 2 insertions(+), 2 deletions(-)
diff --git a/drivers/staging/nvec/nvec.c b/drivers/staging/nvec/nvec.c
index 2823cacde..18c5471d5 100644
--- a/drivers/staging/nvec/nvec.c
+++ b/drivers/staging/nvec/nvec.c
@@ -627,7 +627,7 @@ static irqreturn_t nvec_interrupt(int irq, void *dev)
break;
case 2: /* first byte after command */
if (status == (I2C_SL_IRQ | RNW | RCVD)) {
- udelay(33);
+ usleep_range(32, 33);
if (nvec->rx->data[0] != 0x01) {
dev_err(nvec->dev,
"Read without prior read command\n");
@@ -714,7 +714,7 @@ static irqreturn_t nvec_interrupt(int irq, void *dev)
* We experience less incomplete messages with this delay than without
* it, but we don't know why. Help is appreciated.
*/
- udelay(100);
+ usleep_range(99, 100);
return IRQ_HANDLED;
}
I have zero knowledge about this driver, but nvec_interrupt() seems to be
a hard interrupt handler, and sleeping in an interrupt handler is a big no
no. So I think this change breaks the driver.
Delaying like the driver is currently doing doesn't break things, but it is
not very nice because this is interrupt handler and the processor cannot
switch to other tasks, so delaying is wasting processor's cycles here. The
better fix would be to figure out how to remove the delay entirely, or
switch to threaded interrupt handler and then we can use usleep_range() in
there, but you need actual hardware to test such changes.
the real fix to read back the value we wrote to the controller, similar to
what is done for the tegra i2c host, which is a trival fix.
Unfortunately, this breaks the touch pad initialisation, which needs to be
fixed first. As this topic comes up every year, I'm going to post a patch
in order to updated the comment, so this kind of patches should
(hopefully) stop in the future.
Best regrards,
Marc