Hi,
On 14-03-18 23:16, Lukas Wunner wrote:
On Wed, Mar 14, 2018 at 11:06:02PM +0100, Hans de Goede wrote:
This reverts commit 43fff7683468 ("Bluetooth: hci_bcm: Streamline runtime
PM code"). The commit msg for this commit states "No functional change
intended.", but replacing:
pm_runtime_get();
pm_runtime_mark_last_busy();
pm_runtime_put_autosuspend();
with:
pm_request_resume();
Does result in a functional change, pm_request_resume() only calls
pm_runtime_mark_last_busy() if the device was suspended before the call.
Yes, Robert Howell (cc) reported this a few days ago:
https://bugzilla.kernel.org/show_bug.cgi?id=198953
I've worked with him to develop a fix which is better IMHO than a revert,
namely he's replacing the pm_request_resume() in bcm_recv() with
pm_runtime_mark_last_busy(), and the pm_request_resume() in the interrupt
handler can stay. He says that fixes the issue for him.
It makes the race window a lot smaller, but it still leaves a race:
1) some data comes in, gets full read from the device
2) 4.9999 seconds elapse since last byte has been read
3) new data comes in, triggers IRQ, IRQ does nothing because runtime suspend
has not yet kicked in
4) runtime suspend kicks in, disabling the uart before the first new byte is received
5) stuck again
I hope he'll submit the patch shortly.
We're quite far into the cycle already and this is a serious regression,
also nothing of great value is lost by the revert, the original commit
was a minor cleanup which turns out to have bad side-effects, a simple
revert really is the best solution here, esp. in this point of the cycle.
Regards,
Hans
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