commit 74402055a2d3ec998a1ded599e86185a27d9bbf4 upstream. The pinmuxing was missing for I2C1 which was causing intermittent issues with the PMIC which is connected to I2C1. The bootloader did not quite configure the I2C1 either, so when running at 2.6MHz, it was generating errors at time. This correctly sets the I2C1 pinmuxing so it can operate at 2.6MHz Fixes: 687c27676151 ("ARM: dts: Add minimal support for LogicPD Torpedo DM3730 devkit") For linux-4.4.y Signed-off-by: Adam Ford <aford173@xxxxxxxxx> diff --git a/arch/arm/boot/dts/logicpd-torpedo-som.dtsi b/arch/arm/boot/dts/logicpd-torpedo-som.dtsi index 80f6c78..e056704 100644 --- a/arch/arm/boot/dts/logicpd-torpedo-som.dtsi +++ b/arch/arm/boot/dts/logicpd-torpedo-som.dtsi @@ -90,6 +90,8 @@ }; &i2c1 { + pinctrl-names = "default"; + pinctrl-0 = <&i2c1_pins>; clock-frequency = <2600000>; twl: twl@48 { @@ -137,6 +139,12 @@ OMAP3_CORE1_IOPAD(0x218e, PIN_OUTPUT | MUX_MODE4) /* mcbsp1_fsr.gpio_157 */ >; }; + i2c1_pins: pinmux_i2c1_pins { + pinctrl-single,pins = < + OMAP3_CORE1_IOPAD(0x21ba, PIN_INPUT | MUX_MODE0) /* i2c1_scl.i2c1_scl */ + OMAP3_CORE1_IOPAD(0x21bc, PIN_INPUT | MUX_MODE0) /* i2c1_sda.i2c1_sda */ + >; + }; }; &omap3_pmx_core2 { -- 2.7.4 -- To unsubscribe from this list: send the line "unsubscribe linux-omap" in the body of a message to majordomo@xxxxxxxxxxxxxxx More majordomo info at http://vger.kernel.org/majordomo-info.html