On Thu, 6 Sep 2018 11:11:57 +0000 Yogesh Narayan Gaur <yogeshnarayan.gaur@xxxxxxx> wrote: > Hi Boris, > > > -----Original Message----- > > From: Boris Brezillon [mailto:boris.brezillon@xxxxxxxxxxx] > > Sent: Saturday, August 4, 2018 7:07 PM > > To: Han Xu <han.xu@xxxxxxx> > > Cc: Frieder Schrempf <frieder.schrempf@xxxxxxxxx>; David Wolfe > > <david.wolfe@xxxxxxx>; Fabio Estevam <fabio.estevam@xxxxxxx>; > > Prabhakar Kushwaha <prabhakar.kushwaha@xxxxxxx>; Yogesh Narayan Gaur > > <yogeshnarayan.gaur@xxxxxxx>; shawnguo@xxxxxxxxxx; linux- > > mtd@xxxxxxxxxxxxxxxxxxx; linux-spi@xxxxxxxxxxxxxxx; > > dwmw2@xxxxxxxxxxxxx; computersforpeace@xxxxxxxxx; > > marek.vasut@xxxxxxxxx; richard@xxxxxx; miquel.raynal@xxxxxxxxxxx; > > broonie@xxxxxxxxxx Subject: Re: Questions about the Freescale/NXP > > QuadSPI controller > > > > Hi Han, > > > > On Thu, 2 Aug 2018 21:58:48 +0000 > > Han Xu <han.xu@xxxxxxx> wrote: > > > > > > -----Original Message----- > > > > From: Frieder Schrempf [mailto:frieder.schrempf@xxxxxxxxx] > > > > Sent: Thursday, August 2, 2018 8:09 AM > > > > To: David Wolfe <david.wolfe@xxxxxxx>; Fabio Estevam > > > > <fabio.estevam@xxxxxxx>; Prabhakar Kushwaha > > > > <prabhakar.kushwaha@xxxxxxx>; Yogesh Narayan Gaur > > > > <yogeshnarayan.gaur@xxxxxxx>; Han Xu <han.xu@xxxxxxx>; > > > > shawnguo@xxxxxxxxxx > > > > Cc: linux-mtd@xxxxxxxxxxxxxxxxxxx; boris.brezillon@xxxxxxxxxxx; > > > > linux- spi@xxxxxxxxxxxxxxx; dwmw2@xxxxxxxxxxxxx; > > > > computersforpeace@xxxxxxxxx; marek.vasut@xxxxxxxxx; > > > > richard@xxxxxx; miquel.raynal@xxxxxxxxxxx; broonie@xxxxxxxxxx > > > > Subject: Re: Questions about the Freescale/NXP QuadSPI > > > > controller > > > > > > > > Ping. > > > > > > > > I'm not sure if my message below went out to you at all. At > > > > least I can't find it in the ML archive. > > > > > > > > I still hope someone can help with the questions below. > > > > > > > > Meanwhile for the second point I did some tests myself with one > > > > chip on each of the two buses and it worked fine with my latest > > > > v2 patches. So I'm not sure at all why Yogesh has problems with > > > > his setup (two chips on the first bus). > > > > > > Tried to test the v2 patch set on i.MX6SX SDB board but get the > > > memory map > > failure. > > > > > > [ 1.298633] fsl-quadspi 21e4000.qspi: ioremap failed for > > > resource [mem > > 0x70000000-0x7fffffff] > > > [ 1.307330] fsl-quadspi 21e4000.qspi: Freescale QuadSPI probe > > > failed [ 1.313922] fsl-quadspi: probe of 21e4000.qspi failed > > > with error -12 > > > > > > This is the reason why dynamic ioremap added in previous driver, > > > please refer to > > > > > > https://emea01.safelinks.protection.outlook.com/?url=https%3A%2F%2Fpat > > > > > chwork.ozlabs.org%2Fpatch%2F503655%2F&data=02%7C01%7Cyogeshnar > > ayan > > > .gaur%40nxp.com%7Caed89ff1b0ac4936acd408d5fa0f7303%7C686ea1d3bc2 > > b4c6fa > > > > > 92cd99c5c301635%7C0%7C0%7C636689866643724038&sdata=lZnBc0m% > > 2BOp8yY > > > JBFcNBEa2HSoNMhmJjeM9cIoGeVs0E%3D&reserved=0 > > > > We can reduce the size of the iomap to 2k * 4, since this is all we > > use currently. Can you try to change the size of the ioremap call > > to 16k and tell us if it works. > > > > Unrelated to this issue, we still have 2 questions left unanswered: > > > > 1/ is there an easy way to invalidate AHB buffers? I mean, not > > something that implies a full reset + several milliseconds of > > delay after the reset. Right now we trick the caching logic by > > mapping a portion that is twice the size of the buffer and > > switching from one sub-portion to this other to trigger a real read > > on each read access, but that's hack-ish, and I'd be surprised if HW > > engineers hadn't planned for this "manual AHB buffer flush" case. > > > > I had a discussion with the HW IP owner, they said that IP command > and AHB command are two separate sets of accessing method to flash. > Memory coherency between IP and AHB command can't be maintained by > the hardware. So after every IP data write command (write, erase, > write reg) AHB RX buffer needs to be flushed. > > Software Reset is the safest way to achieve this. > Adding of the delay in several millisecond after setting of the Reset > Bits is too conservative, can be tried with the reduced value. Do you know exactly how many cycles/nanoseconds we should wait? Is there a status reg that says when the block is ready to be used again? > > > 2/ if we use DMA, do you know what happens when the TX FIFO runs out > > of data while the TX request is not finished yet. In PIO mode, it > > seems the engine sends garbage on the bus when that happens, and > > we definitely don't want that. > > For this query, they have said TX FIFO is the max limit, if data send > more than TX FIFO size then it would results in un-defined behavior > and there would be data corruption. Okay. Marek, I guess we have a good reason to accept patch [1] now. [1]http://patchwork.ozlabs.org/patch/928677/ ______________________________________________________ Linux MTD discussion mailing list http://lists.infradead.org/mailman/listinfo/linux-mtd/