On Wed, May 11, 2022 at 11:15:32AM +0300, Ivan Bornyakov wrote: > On Tue, May 10, 2022 at 12:29:54PM +0100, Conor Dooley wrote: > > On 09/05/2022 19:56, Conor Dooley wrote: > > > On 09/05/2022 18:16, Ivan Bornyakov wrote: > > > > On Mon, May 09, 2022 at 11:41:18AM +0000, Conor.Dooley@xxxxxxxxxxxxx wrote: > > > > > Hey Ivan, one comment below. > > > > > Thanks, > > > > > Conor. > > > > > > > > > > On 07/05/2022 08:43, Ivan Bornyakov wrote: > > > > > > ... snip ... > > > > > > +static int mpf_read_status(struct spi_device *spi) > > > > > > +{ > > > > > > + u8 status, status_command = MPF_SPI_READ_STATUS; > > > > > > + struct spi_transfer xfer = { > > > > > > + .tx_buf = &status_command, > > > > > > + .rx_buf = &status, > > > > > > + .len = 1, > > > > > > + }; > > > > > > + int ret = spi_sync_transfer(spi, &xfer, 1); > > > > > > + > > > > > > + if ((status & MPF_STATUS_SPI_VIOLATION) || > > > > > > + (status & MPF_STATUS_SPI_ERROR)) > > > > > > + ret = -EIO; > > > > > > + > > > > > > + return ret ? : status; > > > > > > +} > > > > > > + > > > > > > ... snip ... > > > > > > + > > > > > > +static int poll_status_not_busy(struct spi_device *spi, u8 mask) > > > > > > +{ > > > > > > + int status, timeout = MPF_STATUS_POLL_TIMEOUT; > > > > > > + > > > > > > + while (timeout--) { > > > > > > + status = mpf_read_status(spi); > > > > > > + if (status < 0 || > > > > > > + (!(status & MPF_STATUS_BUSY) && (!mask || (status & mask)))) > > > > > > + return status; > > > > > > + > > > > > > + usleep_range(1000, 2000); > > > > > > + } > > > > > > + > > > > > > + return -EBUSY; > > > > > > +} > > > > > > > > > > Is there a reason you changed this from the snippet you sent me > > > > > in the responses to version 8: > > > > > static int poll_status_not_busy(struct spi_device *spi, u8 mask) > > > > > { > > > > > u8 status, status_command = MPF_SPI_READ_STATUS; > > > > > int ret, timeout = MPF_STATUS_POLL_TIMEOUT; > > > > > struct spi_transfer xfer = { > > > > > .tx_buf = &status_command, > > > > > .rx_buf = &status, > > > > > .len = 1, > > > > > }; > > > > > > > > > > while (timeout--) { > > > > > ret = spi_sync_transfer(spi, &xfer, 1); > > > > > if (ret < 0) > > > > > return ret; > > > > > > > > > > if (!(status & MPF_STATUS_BUSY) && (!mask || (status & mask))) > > > > > return status; > > > > > > > > > > usleep_range(1000, 2000); > > > > > } > > > > > > > > > > return -EBUSY; > > > > > } > > > > > > > > > > With the current version, I hit the "Failed to write bitstream > > > > > frame" check in mpf_ops_write at random points in the transfer. > > > > > Replacing poll_status_not_busy with the above allows it to run > > > > > to completion. > > > > > > > > In my eyes they are equivalent, aren't they? > > > > > > > > > > I was in a bit of a rush today & didn't have time to do proper > > > debugging, I'll put some debug code in tomorrow and try to find > > > exactly what is different between the two. > > > > > > Off the top of my head, since I don't have a board on me to test, > > > the only difference I can see is that with the snippet you only > > > checked if spi_sync_transfer was negative whereas now you check > > > if it has a value at all w/ that ternary operator. > > > > > > But even that seems like it *shouldn't* be the problem, since ret > > > should contain -errno or zero, right? > > > Either way, I will do some digging tomorrow. > > > > I put a printk("status %x, ret %d", status, ret); into the failure > > path of mpf_read_status() & it looks like a status 0xA is being > > returned - error & ready? That seems like a very odd combo to be > > getting back out of it. It shouldn't be dodgy driver/connection > > either, b/c that's what I see if I connect my protocol analyser: > > https://i.imgur.com/VbjgfCk.png > > > > That's mosi (hex), ss, sclk, mosi, miso (hex), miso in descending > > order. > > > > I think what was happening was with the snippet you returned one > > of the following: -EBUSY, ret (aka -errno) or status. Since status > > is positive, the checks in mpf_spi_write.*() saw nothing wrong at > > all and programming continued despite there being a problem. > > > > The new version fixes this by returning -EIO rather than status from > > poll_status_not_busy(). > > > > I wish I had a socketable PolarFire so I could investigate further, > > but this looks like it might a be hardware issue somewhere on my > > end? > > > > So ye, sorry for the noise and carry on! I'll try tofind what is to > > blame for it. > > > > Thanks, > > Conor. > > > > Hi, Conor. > > I've just noticed in SPI-DirectC User Guide [1] ch. 9 SmartFusion2 and > IGLOO2 SPI-Slave Programming Waveform Analysis, that hw status checked > two times every time. Does MPF family also need double check hw status? > Does adding second mpf_read_status() to poll_status_not_busy() routine > help with your issue? Sorry, forgot to insert link to SPI-DirectC User Guide. Here it is: [1] https://coredocs.s3.amazonaws.com/DirectC/2021_2/spi_directc.pdf